Discuss your Trainz adventures here!

bentrain14

does not make bogies
This is mainly for Southern and wannabe and me to discuss some happenings in our railroading careers on trainz. Yes most of the stuff is made up, but it gives more sense to fictional routes and something to talk about. So, if anyone wants to join in (and by join in I mean go along with it all and dont hate/ cause flame wars by being sarcastic) and have fun and share your stories/made up tales. I would love to see the Mods get involved too. :D


So to start it off where we left off, I was telling about how my MOW driver Jerry got lost in KC and wound me up in a yard n Alabama for a while.
 
Also, to set something straight, I met wannabe at the yard, told him if he wanted help I could while Im up there and so I did. Kinda volunteer work if you would say from a bnsf employee. Also I was wondering why his sun gasses looked so dark.
 
Does this include firing AI drivers that don't behave?

I have a few I can add on this!

John
 
Oh gawsh... So after bentrain and wannabe messed up three or four trains in the South Yard in Autumnville on my Alabama & Southeastern RR, I sent a few CEFX GP's to fix their work while I went over to Greenwood to send wannabe to the eye doctor. He handed the Greenwood Local off to a yellow vest out of Montgomery named Doug. So wannabe clocks out and goes to the eye doctor, and while he's gone, Doug drills a car and got a DUI. So I had him in my office to figure out exactly what the heck had happened (between that and the switching mess up and a derailment on Cheaha Pass clogging up traffic, I was not having a good day). Apparently he'd been doing 35 mph (limit on the branch is 25) and spotted it about half a mile away, and was unable to stop. Apparently the guy had been trying to commit suicide, but he survived (Doug slowed down enough so that he was actually just a bit bruised up). So when the train finally stopped, the guy got out, walked over to the engineer side window and flipped Doug off, but the paramedics and cops were on the scene before the guy could get away. Maybe they can get that guy a psychiatrist or therapist or something. So seeing how the accident could've been prevented and it wound up costing us a good bit, I ordered a 3 week suspension. Doug, thinking it wasn't his fault, preceded to flip me, his boss, off. I fired him on the spot. From what I've heard, he got a job with BNSF and was transferred to Kansas City. Ben, if you happen to find a guy up there named Doug Norwood, drop his *** for me.
 
He is one of my trainees. Boy is he getting an A** whooping. Ill start him off repairing an old aloco for yard pushes then go around our big manifest due to leave about 6:00 a.m. and untie the air hoses for him. Ahh the joy of being a veteran in the Railroad. Also to mention a few things u, I formerly worked for BNSF, got a job as head CEO of RAFT rails, went to be lead engineer, then BNSF picked me up for double duty. We are setting up leasing and new trackage around for RAFT and BNSF. Boy it will be fun working out the paperwork for that.
 
Nice! I started out as one of the original engineers on the A&SE, I converted to shop work in 1985 and started climbing the corporate ladder after the old Autumnville Shops closed down in 1993. It's a shame, there's only three rickety tracks and one building left there now, it used to be two buildings and a fueling area, about 7 tracks total. Today I am Head of Operations for the A&SE. Wannabe is pretty much in control of everything on the Greenwood Branch, supposedly he's the yard master over at Greenwood Yard, but he still runs half the switching ops and ends up working the yards down here now and then.
 
Well, paper works holding off for a while. One of our engineers in RAFT passed away today after an exhaust venting problem in one of our engine shops in South Carolina. The shop is closed until further investigation can be brought up. Up in the Russian part of RAFT, we have doubled shipping costs until the Government shut down is over, then after a week or so, prices will return lower than before about 45% shipping costs.
 
Not much to report here, well, conrailfan did kill a guy yesterday on the golf course running next to the A&SE mainline. He was aiming for the green on a Par 4, and ended up drilling a guy in the head...a full 200 yds from where he was aiming. I have officially banned him from golf.

In other news, the wreck I reported 5 days ago was just outside a tunnel. We have a nightmare scenario going on. It's a 467 ft long tunnel, and between the wrecked well cars & containers as well as the assorted cars from the other train, it's going to be a very slow clean up process. Then we will have to repair any damage done to the tunnel. The Pass will be completely shut down until all of that is done, the yard at the base of the pass is at capacity, the yard in Montevallo is at capacity, and Autumnville is rapidly getting weighed down with overflow traffic as well, and the next few yards probably won't last long either, on the other side of the pass Oak Mountain Yard is at capacity, and the Birmingham Yard has never been this close to capacity before. If Birmingham has to overflow traffic to the next yard we're in trouble. The A&SE crew has been working tirelessly at the cleanup, but another crew is hard at work repairing the West Side Line. We created it in 1997 as a bypass to Cheaha, but while the grades were gentler, it was a longer and less well-built route, and we discontinued use of it in 2008. If we can get it fixed up enough to relieve some of this congestion, the line we used to think of as useless might just save our ***es. In the mean time, I have to oversee the repair of the units involved in the wreck. A&SE SD44-2 8481 and SD39M 3844 both suffered pretty severe damage when they collided nose to nose, SD44-2 8497 has minor damage from rolling over, SD33-3 3320 has rear pilot damage, and SD42-3 7179 just about had its cab ripped off when it got slammed into the tunnel portal form the impact. It's in the worst shape of the bunch and will take a pretty massive overhaul to fix, it'll need a new nose and cab, a new front pilot, a new front bogie, a new fuel tank to replace the damaged one (no leaks, but it's pretty banged up), a new inertial filter hatch, as well as various other body repairs. This is going to be an expensive accident for sure.
 
Before some idiot comes in and says "this thread is stupid lock it please"....


So apparently some drunk knucklehead ran the gates in Pennsington late last night. The local L924 (affectionately known by the crews as the Guardian Local), pegged him, resulting in a major response. Guy was lucky he didn't die, and had to be pried out by PFD Squad 3 and Engines 69 and 17 (who were less than a mile down the street). Photos soon...


Oh, almost forgot: This is a really nice idea. Imagine all the stories we can create with two hours and some stupid AI drivers! :p
 
XD

Well, we ran a small local freight over the old roundabout line to see how much progress we were making. It derailed when the roadbed collapsed from under it about 15 miles in. Back to square one...
 
Hi, i'm the CEO of the Rice Creek Railway a a class 2 railroad that serves the Midwest. I started as a engineer 8 years ago and have risen up the ladder slowly, becoming CEO 7 months ago. The actual story later tonight.
TJ
 
Nice hope to hear more. On our side, I was visiting the Mojave on another volunteer trip to help out some trainee engineers for Union Pacific. So two knuckle heads thought it would be funny to run a curve at 15MPH, then Highball over a switch. Well, in other news, they are permanently fired, cause they died, and clean up took about 3 days and another 6 trying to find left over pieces of the engineer's right arm, and left thigh that got torn up from the metal then blown 150 yards down the main from an explosion in the diesel tank. About 900,000 dollars in damage and 10,000 dollars in funeral costs.
 
Alright, On the weekend's we operate excursions across the countryside behind our RS27s. Well the 2 27's required to pull the excursion are scheduled to leave the Engine facilaty at 5:00AM to head to the Mone River City passenger terminal 5 miles away. The first excursion is at 10:00 but they have to cross the NS line and that can take hours. Well at 3:36AM on Saturday NS had a small derailment on the diamond lead units truck on the ground no problem, be cleaned up in an hour right? Wrong. Turns out that some guy had chopped the rail to cause the derailment and now the local Cops were involved. So NS was not allowed to move the train off the diamond. Now were up a creek with no paddle in sight. I called the western division manger Joe and ask him to find two units that are free and send them to Mone River ASAP. He tells me all he has is a GP30 & a SD45 in East Haven that are free. I tell him get a crew and tell them to highball to Mone River. East Haven is 70 Miles from Mone River and it's a 2 and a half hour run, They highball to Mone river and arrive at 8:51AM an hour and nine mintues till departure of the first train. Just another day on the Rice Creek.
TJ
 
We were running downgrade from Cresson, which is shortly thereafter almost flat and level trackage.

With a consist well over 6000' in length, having 15,000 tons of TTX piggyback trailers behind us, when we started through the New Portage bore. I put the train into the throttle 1 position, and by the time we had reached the Tunnelhill side of the bore, most of the train weight was now cresting over the summit of the -1.87% grade.

Putting the loco throttle to the zero position, and applying the 50% dynamic brake setting, I slowly put the loco throttle into the notch 6 position, which slowed the train somewhat.

The rear end helpers now also crested over the summit, and the entire train weight was bunched up, with the slack run in. The train was increasing in speed all along the sweeping Salpino Curve, and by the time we reached Bennington Curve interlocking, I had put the dynamics into the notch 8 position, and applied several notches on the service brake application. The train speed was ever increasing past 35 mph, and by the time we had passed Allegripus Curve, the train was beginning to become out of control. Trying to avoid a full emergency braking application, that could cause a run-in derailment, I further applied the service brake, until we had a full brake application.

Moving the throttle to zero, I applied the 100% dynamic braking, and put the throttle quickly back into the "Run 8" position.

The train was now at 45 mph, and approaching MG tower we informed Alto tower that we were now a full fledged run-away, and our trainline air pressure had been Psssssst away in our multiple service brake applications.

We now attempted full emergency braking, as we came within sight of the Horseshoe we were doing 55 mph. Hold on, and brace yourself I cried to my conductor, or make like the birds, and jump (NR at 55 mph).

By the time we reached MP 241.7 we were doing in excess of 65 mph, and shortly thereafter we derailed, blocking the entire 4 track main, with 28 derailed TTX Piggyback flats of US Mail. Some trailers flipped and ripped open, and US Mail was all strewn all over creation, down over the steep, rattlesnake, copperhead and stickerbush infested hillside (and each and every piece of US Mail had to be personally retrieved by a small army of leatherneck workers, using rope harness's and winches).

Within several hours only one track (the #4 track) had been hastily repaired, and opened for operation through the derailment site.

This, did in fact occur, on the prototype on several occasions through out the history of the Horseshoe, the last being @ 1993.

Just some other notable accidents were: The steamer boiler explosion at SF tower fatally injuring the tower operator (portions of the boiler were hurled 1000' into the air, coming to rest 3/4 mile distant), Bennington Wreck of the Red Arrow, Allegripus fatal wreck of a steamer (named Allegripus) that plunged down over the cliff side, and the TTX piggyback trailer US Mail train wreck at Cold Curve.
 
Nice hope to hear more. On our side, I was visiting the Mojave on another volunteer trip to help out some trainee engineers for Union Pacific. So two knuckle heads thought it would be funny to run a curve at 15MPH, then Highball over a switch. Well, in other news, they are permanently fired, cause they died, and clean up took about 3 days and another 6 trying to find left over pieces of the engineer's right arm, and left thigh that got torn up from the metal then blown 150 yards down the main from an explosion in the diesel tank. About 900,000 dollars in damage and 10,000 dollars in funeral costs.
$10,000 in funeral costs for two people?!? Those are some cheap*** funerals.
 
$10,000 each. A little more but that basically sums it up. Explosion still being looked into and now they are being sued by the conductors family saying "the equipment wasn't well maintained by the railroad" no matter how many times we show the cab cam footage. Most likely though, because they have the footage, they wont get to far in suing. THANK GOD FOR CAB CAMS!
 
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